Well I now have a 3500 in the car due to a head gasket going on the 3400 only a month after I did the LIM gaskets.![]()
The 3500 is the one out of my old Alero, it has ported heads, 3400 head gaskets, ported rear exhaust manifold from the 3400, LIM gasket matched at the heads, stock 2000+ plenum, 56mm TB, 97 3100 injectors on a 2000+ fuel rail/regulator and yes still on a stock 3.1mpfi tune!
The track sucked, little to no prep, 100% humidity, 12-13*c, 30km/h head wind! the 3500 pulls harder down low compared to the 3400 resulting in worse 60 ft's than last time. barely ran a new best of 15.609 @89.80mph. Ran lots of 15.7 and 15.6's.
slip:
rt ... .295
60' ... 2.375
330... 6.557
1/8... 10.080
mph...70.40
1000...13.082
1/4...15.609
mph...89.80
Going to go back next friday as long as the weather is good, with the 65mm TB installed and possibly 2.5" cat back. The 56mm TB, 2" exhaust and tune are really holding this thing back!
here is an in car vid from the track of one of the slower runs! You can see how bad the car floats in the top end! (needs sturts bad!)
http://www.youtube.com/watch?v=JUn8rcdEft4



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